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DMC-2X00 
Chapter 9 Troubleshooting  
y 131  
Communication 
 
SYMPTOM CAUSE 
REMEDY 
Using terminal emulator, cannot 
communicate with controller. 
Selected comm. port incorrect 
Try another comport 
Same as above 
Selected baud rate incorrect 
Check to be sure that baud rate 
same as dip switch settings on 
controller, change as necessary. 
Stability 
 
SYMPTOM CAUSE REMEDY 
Motor runs away when the loop is 
closed. 
Wrong feedback polarity. 
Invert the polarity of  the loop by 
inverting the motor leads (brush type) 
or the encoder. 
Motor oscillates. 
Too high gain or too little 
damping. 
Decrease KI and KP.  Increase KD. 
Operation 
 
SYMPTOM CAUSE 
REMEDY 
Controller rejects command.  
Responded with a ? 
Anything. 
Interrogate the cause with TC or 
TC1. 
Motor does not complete move. 
Noise on limit switches stops the 
motor. 
To verify cause, check the stop 
code (SC).  If caused by limit 
switch noise, reduce noise. 
During a periodic operation, motor 
drifts slowly. 
Encoder noise  
Interrogate the position 
periodically.  If controller states 
that the position is the same at 
different locations it implies 
encoder noise. Reduce noise. Use 
differential encoder inputs. 
Same as above. 
Programming error. 
Avoid resetting position error at 
end of move with SH command.