Справочник Пользователя для Mitsubishi Electronics QD75MH2

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Appendix - 56 
MELSEC-Q
 
APPENDICES 
 
Trouble type 
Questions/Trouble 
Remedy 
No. 
Backlash compensation value 
     0 
≤ 
Movement amount per pulse 
≤ 65535 
Error 920 (backlash compensation 
amount error) occurs even when 
the backlash compensation value 
is set to "1". 
Setting is not possible if the above equation is not 
satisfied.  
45 
When a JOG operation is 
attempted, errors such as error 
104 (hardware stroke limit+) or 
error 105 (hardware stroke limit  ) 
occur and the machine does not 
move. 
The hardware stroke limit wiring has probably not been 
carried out.  
Refer to section "12.4.4 Hardware stroke limit function" for 
details, and wire accordingly. 
46 
Error 997 (Speed selection at OP 
shift error) appears when the PLC 
READY signal [Y0] turns from OFF 
to ON. 
A value besides "0" or "1" may be set in the  Pr.56  Speed 
designation during OP shift. 
Review the set PLC program, and reset the correct 
parameters. 
47 
When the start signal was turned 
ON immediately after the stop 
signal ON, warning 100 (start 
during operation) was detected, 
and the start was ignored. 
The QD75MH starts the deceleration stop process when 
the stop signal ON is detected. Thus, the machine 
interprets that "positioning is still being executed" 
immediately after the stop signal ON. Even if the start 
signal is turned ON at that time, the start request will be 
ignored and warning 100 will occur. 
48 
Error/warning 
Does warning 500 (deceleration 
and stop speed change) occur 
only during "stop deceleration" and 
"automatically deceleration"? 
Is there any problem if the 
operation is continued in that state 
without resetting the error? 
The warning occurs only at those times mentioned at the 
left. Because this is a warning, there is no problem if the 
operation can be continued without resetting the error.  
(When the speed is changed using the override, the new 
value will not be reflected on the data being executed, but 
will be reflected from the next start.) 
49 
The positioning may have not been completed properly  
by the occurrence of the stop factor. 
Check the axis monitor "
Md.26
axis operation state"  
after BUSY signal OFF. 
Stopped                          : The stop signal is turned ON 
during positioning. 
Check the condition of the stop 
signal (Y stop or external stop) 
ON. 
During error occurrence : An error occurred during 
positioning.  
Check the cause of error 
occurrence from "
Md.23
 axis 
error number". 
50 
Positioning 
completion signal 
When the position control is 
carried out, the positioning 
completion signal is not turned ON. 
The setting value for detailed parameter 2 "Positioning 
completion signal output time" is 0 or shorter than scan 
time. 
Set the properly detectable time using the PLC program. 
51