Magnetek TM7310rev01 Benutzerhandbuch

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Quattro DC Troubleshooting 
 
Name Description 
Possible Causes & Corrective Action 
Field 
Overcurrent 
 
An over current condition has 
been detected in the field 
circuit by the hardware. 
Check Parameter Settings 
 
Verify parameter settings for motor field control 
Check motor field and wiring 
 
Check motor field and wiring for short circuits 
Full Fld Time  
 
Drive was commanded to 
provide Full Field current but 
not told to Start for longer than 
the time set in FULL FIELD 
TIME (A1) 
Incorrect Start Timing 
 
Check for proper drive Start sequencing 
signals  
 
Verify FULL FIELD TIME (A1) 
Hit Current Limit 
(alarm) 
 
The drive is or was being 
limited by the motor current 
limit setting.  This can limit 
acceleration rates and cause 
subsequent velocity tracking 
errors. 
Incorrect Wiring 
 
Verify motor armature circuit wiring 
 
Verify motor field current is correct 
Drive and/or Motor is Undersized 
 
Verify drive and/or motor sizing.  May need a 
larger capacity Drive and / or motor.  
Check Parameter Settings 
 
Check the torque limit parameter MTR 
TORQUE LIMIT (A1) 
 
Check speed regulator parameters 
RESPONSE and INERTIA (A1) 
 
Alarm sensitivity - TRQ LIM MSG DELAY (A1) 
parameter determines the amount of time the 
drive is in torque limit before the alarm 
message is displayed. 
HW/SW 
Mismatch 
 
Line side software is installed 
in the motor side control 
board. 
Incorrect Software in Motor Side Board 
 
Replace A2 board with correct software for 
board location or program correct software into 
Motor Side Board 
Invalid 
Checksum 
(operator serial 
link error)
 
The operator received four 
consecutive invalid messages.
Noise or Bad Connector Connection 
 
Remove and re-seat the operator in its cradle. 
 
If re-occurs, the operator or the drive’s control 
board may need to be replaced. 
IP Comm 
 
A fault has occurred in the 
communications channel 
between the Line side and 
Motor side processors.  This 
was detected on the motor 
side. 
Communication problem 
 
Reset drive 
 
Verify Line Side software and Motor Side 
software is compatible.   
 
If re-occurs, replace Main Processor PCBs 
Line HI Volts 
 
Line voltage is greater than 
552 VAC.  (480 x 115%)  
Monitored via the DC Bus. 
Line Voltage is too High 
 
Verify DC Bus is reading voltage correctly 
 
Verify Line voltage is set correctly 
LS A to D 
 
The Analog to Digital 
conversion on the line side 
control board is not working 
properly. 
Line Side Analog to Digital Conversion 
incorrect 
 
Replace Line Side Main and Power Interface 
PCBs  
LS AC CNTCR 
 
The main AC power contactor 
is not following the 
commanded state within 1 
second. 
AC Power Contactor Problem 
 
Check for faulty UTM contactor coil or 
interlocking aux contact blocks on PCM or 
UTM 
 
Verify that pilot relay K2 on PCB A8 is working 
properly 
CAUTION: Do not manually engage the UTM 
contactor with power applied.  
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